| Self Righting Boat |
|
|
| Monday, 04 December 2006 | |||||||||
|
Misc. Article ...by Rudy Hilado
An amazing boat that sets itself right side up after a flip!
I learned that electric boaters have been exploiting this ability for some time, especially the European boaters (See http://www.rc-raceboats.de/), but I wasn't aware of anyone trying to incorporate self-righting properties in a gas powered boat.
A Tide Channel
A tide channel is a large cavity built into one side of the hull, running nearly the whole distance from the transom to bow. When the boat is upside down, the channel fills with water causing that side of the hull to sink. This shifts the center of balance and eventually the weight of the motor causes the boat to continue rolling and "pop" right side up. The tide channel is open at the transom, so when the boat rolls over and the prop gets back in the water, the forward movement of the hull causes all the water to pour out of the channel and the boat is off and running again.
There are several challenges that must be overcome to make a gas boat self-right. Electric boats have the luxury of being able to be completely sealed apart from the tide channel, but gas boats require air to get to the carb, and a method for the exhaust to leave the boat, and this has to work right side up, upside down, and during the rolling process. So I picked up an old hull and I began to experiment. I modified a 48" Aeromarine Challenger to have a "tide channel" You can see that I hacked a bit on this hull, making some holes and then covering them up again with duct tape.
I decided to have the boat roll on the port side. This matched the rotation of the prop, which can assist in lifting the port side when righted. Unfortunately the tide channel would then occupy the space where the tuned pipe would typically sit. I handled the exhaust issue by routing the output through the front of the boat and out the starboard bow. This gets the tuned pipe out of the tide channel area, and it keeps the exhaust exit free while the boat is rolling.
The other problem is getting air to the motor. Since the top of the boat needs to be water tight (I wanted the boat to roll, not become a buoy or an anchor! Ooops, that happens later!), I created ventilation holes in the bow of the boat. These holes are above the waterline when the boat is upside down and they provide a good supply of air to the carb.
After much cutting and hacking...
In the end it worked fairly well. The most difficult part of this project is trying to make the hatch fully waterproof. It still leaks a little, but the water drains out pretty quickly (using one of those much maligned auto-bailers).
With this size hull, I think the port side of the engine rail didn't have enough volume to hold enough water to cause the boat to roll (or roll fast enough), so I had to move the radio box components to the starboard side of the engine rails and make the area in the back (where the radio box is typically placed) part of the channel. This allowed a lot more water to get in and roll the boat as well as drop the transom.
For the forward exhaust, I used a flexible stainless steel gas pipe (used with clothes dryer appliances) mounted to the end of the tuned pipe. The exhaust can be optionally routed to exit out the starboard side of the transom, since it doesn't get wet there either, but it's a bit harder to get it to that location because the exhaust port on the motor is on the left. An additional benefit to routing the exhaust so it comes out near the bow is it allows the pipe to fit completely within the boat and you can use a 90 degree header. The standard configuration for an "in the hull" pipe is to have it exit out the transom, but this often requires a long "wrap forward" header to make the pipe fit, with several inches of the pipe hanging out the back. If the pipe is in the hull pointing toward the bow, you can use a shorter 90 header, which can increase the performance of the motor.
Proper venti lation makes a big difference in the performance of a boat. Running with a hatch and very little air moving through the hull will really slow you down. I first tried a big vent on the top deck, but it was too easy for water to go in there when capsized. Instead I cut out vents in the freeboard near the nose of the boat. I over cut it a little bit, but water never got in through the nose vents. To let the incoming air move through the hull, I also cut a hole in the right of the transom to provide an air exit point.
The rollover pro ss still took a little too long (it's not a good idea to have the motor run upside down for a long period with no water going through the cooling jacket), so I think additional holes along the tide channel on the top deck will help the water get in there faster. Also it's important to use an IV bag fuel tank or a fuel tank with a clunker. The motor has to get fuel when it is upside down and the regular tanks donut handle this well.
Occasionally when the boat rolled over, the motor would stall due to sudden load on the prop (which kind of defeats the whole self-righting concept!). I think this problem would be solved if I incorporated a clutch.
Also, running the mo tor without any cooling when it is upside down is not desirable. I think this problem can be solved by incorporating a water pump to push water through the jacket when it is upside down. I believe I know how to make this work, but I'll leave it up to the reader to imagine the possibilities. :-)
Experiment, try out that wacky idea you have, but most of all...have fun!
(read more about the fate of this boat here)
Special thanks to Marty of www.martysrcboats.com for hosting the original post on this project.
|
|||||||||
| Last Updated ( Wednesday, 12 March 2008 ) | |||||||||
Discuss this item on the forums. (0 posts)








